Customer Support 7 days a week

Welcome Guest! You can not login or register.

Notification

Icon
Error

Options
Go to last post Go to first unread
PhxVerde  
#1 Posted : Monday, November 16, 2009 11:05:56 AM(UTC)
PhxVerde

Rank: Member

Groups: Registered
Joined: 11/16/2009(UTC)
Posts: 3

Is there a trick to installing a new wigwag in an older Kenmore washer? I got the old one out with some difficulty, although neither the old wigwag or the shaft show any signs of corrosion. I noted the split in the end of the shaft and thought the new one would slide right on, but I cannot get it to go down at all. Due to the location in the machine, it is very difficult to apply much downward pressure on it. Any ideas would be greatly appreciated!
Sponsor
See inside of your appliance - diagrams and part photos for virtually every model.

powered by AppliancePartsPros.com
 
Gene  
#2 Posted : Monday, November 16, 2009 1:42:12 PM(UTC)
Gene

Rank: Advanced Member

Groups: Senior Expert, Administrators
Joined: 7/19/2007(UTC)
Posts: 27,455

Was thanked: 4 time(s) in 4 post(s)
Have you removed the locking screw from the old wig-wag? Do not screw it in the new part until it is in place. Make sure the plungers shafts are positioned in the right directions (into the solenoids).

Tilt the washer to the front and put some supports under the rear legs. You can adjust the shaft position by slowly moving the belt is any direction.

Gene.
PhxVerde  
#3 Posted : Tuesday, November 17, 2009 6:11:48 AM(UTC)
PhxVerde

Rank: Member

Groups: Registered
Joined: 11/16/2009(UTC)
Posts: 3

Thanks Gene for your suggestions. I have not started the locking screw yet and the plunger shafts are started up into the solenoids. I finally got the wigwag started down on the shaft by employing a crowbar and a piece of 2x4. That thing fits so tight on the shaft I can't imagine even needing the locking screw. By pulling up on the crowbar with all my might, enough to lift the rear of the machine off the ground, I was able to get the wigwag to probably 3/16" of where it needs to be. I hope I don't pull the entire transmission off the machine with all the effort required to slide the wigwag on. I have even lubricated the shaft to try and get the wigwag to slide easier, but I don't think it helped much. Seems like it would have helped to have the hole in the wigwag be just a bit larger in diameter.
Gene  
#4 Posted : Tuesday, November 17, 2009 10:09:48 AM(UTC)
Gene

Rank: Advanced Member

Groups: Senior Expert, Administrators
Joined: 7/19/2007(UTC)
Posts: 27,455

Was thanked: 4 time(s) in 4 post(s)
If it's not too late you can file the shaft with a fine file or a sandpaper. It would not damage the shaft.

Gene.
PhxVerde  
#5 Posted : Wednesday, November 18, 2009 12:33:58 PM(UTC)
PhxVerde

Rank: Member

Groups: Registered
Joined: 11/16/2009(UTC)
Posts: 3

Thanks Gene for all your helpful suggestions. Early this morning, while the metal in the shaft was in a contracted state from the overnight coolness, I was able to finally force the wigwag on the rest of the way, secure the locking screw, and reattach the wires (in the right order!). The machine still ran after all the abuse I have been giving it, and what's better, the spin cycle actually works... Yeah!
Gene  
#6 Posted : Wednesday, November 18, 2009 12:56:51 PM(UTC)
Gene

Rank: Advanced Member

Groups: Senior Expert, Administrators
Joined: 7/19/2007(UTC)
Posts: 27,455

Was thanked: 4 time(s) in 4 post(s)
You are welcome. I'm glad you were able to fix it. Good job!

Gene.
Users browsing this topic
Guest (3)
Forum Jump  
You can post new topics in this forum.
You can reply to topics in this forum.
You can delete your posts in this forum.
You can edit your posts in this forum.
You cannot create polls in this forum.
You can vote in polls in this forum.